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Fixed it! One of the replacement injectors I bought was faulty!! Even though the ohms Reading was correct it still wasn’t right. I tested some old ones I had, found one with the right reading of about 15ohms and switched it out. Bang on!
So mines still the same, it’s had new injectors, new plugs, new leads, new coil and just swapped around the two lambdas. Still the same, it’s pot 3 that’s giving me greif not pot 4
Yes I swapped the injector plug over to see if that did anything, proved the harness was playing the injector. Then swapped injector over and was the same.
Plugs are ngk OEM spec, platinum oft or whatever it is, but correct spec anyways.
172 cup.
Was running fine and after being sat on the drive for about 3 to 4 weeks it developed a missfire.
It had new OEM leads and new ngk laser plat plugs.
Eml flashing and then solid, stinks a bit.
I pulled 2 of the injectors and found them to be a bit dodgy so replaced them
Obd brings...