2011 August –December
Bedford was the last trackday that the Cup would attend in 2011.
I thought it was now time to start looking to advance the car in terms of its track setup, using Nicks Cup as inspiration. His wider track and significantly more negative camber gave him the edge at Brands. His RS2 Extra was also a very handy addition but I wasn't going to be fiting one of them anytime soon.
Now we all know how Cliosport goes through fashion trends and how certain mods come in and out of favour and I’d be daft to say that the Cup hasn’t been tweaked in ways that reflect the trends (2118’s anyone?) but I’ve never been one for modifying the car just for fashion rather than function.
It’s also interesting to see that there are now two quite different ‘acceptable’ ways to approach track work in Clio’s, those being to either leave it totally standard or turn it into an out and out race car.
Now the latter is in no doubt a highly expensive and time consuming venture to take on in whatever spare time you have (unless you hand the car and big wad of cash over to a company to do) and will inevitably produce a car capable of beating up most of the other cars out there on a track day or be capable of mixing it with the front runners in whatever race series it may be entered in.
But, as I say, it ain’t cheap. I should know…..
The Cup has never been tracked in standard form and the nostalgic side of me misses the way the car looked when it was standard.
I also believe it might have been just as fun, if not a touch slower, compared to how it is now but I don’t for one second regret doing what I’ve done to it, even if it is only a kind of a halfway house (or maybe that should be just a third) between being totally standard and a fully blown track/race orientated car.
Money has always been a factor in deciding whether or not to go the whole hog, I’m not a high roller, but that’s not to say I’ve been stingy with the quality of the mods I have made!
You just have to hunt for the bargains…..
Anyway, I digress….
Being friends with several guys who have made rather tasty changes to their cars is highly advantageous…..because it allows someone like me who, after 7 years still isn’t bored of my French tin can, to gain from when the others inevitably do get bored, break and/or sell (and then later regret!) the cars they have played with.
As such the Cup gained a pair of OMP 3 inch harnesses from when James (previously JMS, now Stone) decided that he would break his Ph2 172.
These were actually fitted much earlier than late 2011 but as per normal, I forgot about them earlier….
It was also around about this point of the year that Nick had decided that his Cup, now without its loom and with what seemed to be a fried ECU, was a lost cause and would cost too much money for him to get it back to its former antisocial self, so he also decided to break the car for its component parts.
A perfect opportunity I felt to gain the stance and extra track width that the car lacked, so his front Eibach 25mm and rear 15mm spacers were snaffled along with his used but still serviceable stud kit.
What I hadn’t considered up to this point was his rather rorty Longlife cat back system…..
Now those who knew the Cup well and who had been inside it when I’ve been giving it beans, or who have driven it hard themselves, had all said the same thing about the sound that the Prospeed stealth made in that it sounded not too dissimilar to the R26.R from inside the car. Apparently.
Personally I rather liked it because it was never too intrusive…until the bloody stealthly applied Overrun Map that is.
That said, I was now a little bored of it. The car was always tagged as the 'quiet one', even when the decat was fitted.
And the back box fitted crap. And the hanger broke.
Cue Nicks ex exhaust. Similar in style to the OMP Inox, a little rougher around the edges but just as noisy, and combined with the yet to be removed pops and bangs, pretty antisocial.
Come September the car was living a fairly quiet time (well…I say quiet, its just plain loud now) so with the October Surrey Rolling Road coming up I decided to put it on the rollers and see if the car still had the 177bhp it had back in 2010.
The day was hot. Not autumnal pleasantly warm, but 27 degrees hot.
We turned up typically late on. Which was lucky as all we’d missed were a fleet of Mk1’s….
The Cup went on dead last. I predicted something in the region of 178 but being the stubborn mule that it is it pulled a 176.4…or something like that.
So pretty much the same as last time. Again, stubbornly consistent but it was agreed by all that the noise it made on the rollers in the confines of that old munition building was epic.:approve:
October turned into November and as yet I hadn’t collected let alone fitted the spacers and stud kit from Nick who was kindly holding them for me.
I was in no rush as I had a plan to SORN and hibernate the car for at least January so that I could get several things done on the car that I had been meaning to do for a while.
Things were fairly uneventful until one weekday morning in mid November when I had he beginnings of my first EVER mechanical fault with the car.
Apologies if this bit rambles on a bit.....I like to story tell. You may have noticed...
The car rarely gets used on the commute now so I decided to give it a run out for two days.
Over the previous 7 years I’ve replaced worn bits, and upgraded things but the engine itself has never wanted for anything.
It has always nearly been run on Optimax/V-power which therefore made me suspicious of Tesco 99 when the car, one cold damp morning, suddenly misfired as I drove it to work.
I had decided to put Tesco 99 the evening before purely out of convenience as its closer to work, so my first suspicion was that the car didn’t like it.
Unlikely but not unreasonable.
I had also had my reservations about the fuel pump. Having a stripped rear end means that you can obviously hear more things happening from the back of the car and the fuel pump priming isn’t exactly quiet, but mine has always had a strange a trait.
It never seems to prime on the first turn of the key when cold.
It usually requires a second turn from ignition on, back to off and then on again.
As a precaution against the possibility that both the fuel and fuel pump being the culprits I ‘borrowed’ a spare fuel pump from Mike, ran the tank to nearly empty and then and then topped the tank up with V-Power. This seemed to cure the problem.
Or so I thought.
I was due to work that Saturday and when I left the house it was damp and foggy.
Like every street we have a resident ‘wideboy’ (other than me). He drives a BMW 318 Compact. Badly. Usually about 2 feet from the bumper of the car he’s following, which on this morning was me.
Now it’s a 30 mph limit out of my village and out of pure annoyance to the numpty now sat in my spare wheel well, I stuck to it.
I behaved until I left the roundabout outside the village. Then I booted it.
Now does anyone want to hazard a guess as to when the misfire reared it ugly head again?
Yup, that’s right, just as I pulled second gear. Boll0cks. I sheepishly pulled into the petrol station 100 yards further down the road.
Blip the throttle. Still there. Blip it harder. Wake the neighbours.
I decided to limp on to work and hope it clears on the run up the A3. It did. For about a mile.
Arriving at work it was no better so I decided to start pulling things apart to see what could be the problem.
First suspicions were the simple stuff. Leads and plugs. These appeared clean and in working order as was the MAF sensor.
I eliminated the Lambda purely because there wasn’t an MIL lamp up and I know the symptoms of one going as the Mrs 182 had one go.
Had to be the coilpack.
Quick call to Nick had him winging over with two spares. Hero.
First one tried. Same. Second, same still. Oh come on…..
This needed James’ expertise. He suspected an injector had gone so told me to bring it over to MWM so he could have look.
Nick offered to run home to collect his spare injector rail from the remains of his Cup. Double hero.
By the time I left work to drive it up to MWM the fog had cleared and it was quite warm, and yes, you guessed it, no misfire.
Regardless, James plugged in the RSTuner and soon diagnosed an injector fault on cylinder 2. This was swapped for one that Nick kindly donated and since then (fingers crossed) all has been well.
As the end of the year neared, so did the end of its 6 months of tax which was due to expire on the New Years Eve.
I had planned to hibernate the car at work over the Christmas break and then most of January.
This would allow me to fit the spacers and stud kit as well as a pair of new lower arms, the ball joints long overdue a refresh, and for my brother Ross to set about repainting the front end.
I’d had this in my mind to be done as my brother had progressed as a painter…..he was now being allowed to paint the Aston’s and Lotuses that came through so I felt he was now suitably qualified to take on the Cup…
The front bumper was especially bad, being heavily stone peppered and having been subjected to a pretty poor ‘SMART’ repair at some point in its life that had began to peel away.
The bonnet was also pretty tatty and bearing a couple of dents.
We also decided to blend the front wings to make sure the whole front looked fresh. So the car was tucked away as we broke for Christmas.