Update:
Ok on Thursday the 2nd, I headed off to RS Tuning in Leeds. My family didn’t want me to go, as all they saw on the news was people getting stuck up north on the roads. But I was inpatient and wanted/needed my remap. So my sort of sensible hat came on, and I packed the car with the following:
-Sleeping bag
-Big shovel
-Water
-Food
-Big empty bottle
I said to the family I’ll check the traffic websites before I set off, but at 5:15am I was like a zombie and just headed for the M5. All was going well until I got to the M1, just before the Sheffield junction I got stuck in a traffic jam, due to a car transporter falling over. I was doing so well up until then, after 40 minutes waiting, I really needed to go to the loo, so out came the big empty bottle
Traffic Jam:
Started snowing:
Over an hour had gone by, I called Paul and explained the situation and he was cool with it. Then a lorry moved in lane 1 (I was in lane 2) so this enabled me to move to lane 1. Now I had stopped literally at the slip road to get off to Sheffield. I thought sod it, I’ll get off and see if I can get back on, or if it’s really bad head home. I was kicking myself when I got to the top of the slip road, silly me didn’t think about all the other traffic trying to get onto the M1 for an hour, so at the top of the slip road was a nightmare. I could only go left towards Sheffield, started to think to myself WHY didn’t I just listen to the family at this point!!! There was cars and lorry’s everywhere, abandoned, so I slowly made my way towards Sheffield, I was doing 20mph maybe less, I was causing a queue behind me, but thought sod it, I’m taking my time.
Looked on the sat-nav, zoomed out and I could see the M1 bent to the left and around Sheffield a bit, great I thought I can get back on. So 20 mins later I start seeing signs for M1, spot on. Got back on and headed back to Leeds, and got there after 5 hours in total.
check out the front plate
Pauls colleague washed my car off (thumbs up) and in it went. Got the car mapped, and then went home, got home in 3 hours.
Car ticked over to 58k so thought I’d take a snap
This is not 80mph as i'm on 15" wheels = crappy mpg also :dapprove:
Ok the part most of you want to see, the
results:
As you can see from the results my engine gives up at 6500rpm, but the torque curve Is good. For some reason or the other my car is around 10bhp down, which is obviously linked to whatever is causing the engine to give up at 6500rpm range. Sent the graphs to Tom at JMS who looked at them, then called me back. Tom advised that he was very impressed with the torque curve and is a sign of a healthy engine. Tom said he will need to have my car back, to take a look at what could be causing this issue. A few things he suggested that could be causing it:
-A small blockage somewhere, maybe in the exhaust, filter or somewhere.
-Low compression in the engine, and is this linked to the small oil leak I have?
-The fact I’m running 15” wheels make any difference, had Paul calculated this factor when mapping?
I just need to get the car back to Tom now. But tbh I don’t drive to the limiter often at all, and the low down grunt is very addictive. But I’ve paid for this mod/power so I want to get it sorted. For those interested, the best way I could describe my car now after the rs2, de-cat, uprated engine mounts fitted, is ‘RAW’ & 'exciting'. I still get the odd throttle response delay from 1st gear to 2nd, but only very minor and mainly when the engine is cold and not warmed up yet. I have also noticed since first getting the car from JMS, that the steam coming out of the exhausts, well it only really comes out of the left tail pipe. Is this another sign of a small blockage? Something isn't quite right.......
Thoughts / comments / suggestions welcome