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Daily dci



Brigsy

ClioSport Club Member
  T.Turbo
Updates.

Orange clio has been daily for last 3 weeks. Its running great, done almost 1500 miles in it.

Blue dci mot runs out this week. Front tyres were low with them on the wear bars on inner/outer and 3mm or so in the inside. I reckoned up and i think ive done around 35'000 on the Michelin Crossclimates which is awesome value for money. So on with a fresh pair of Crossclimates ready for winter use.

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Mot booked for Friday am.

Thanks for reading!!
 

Brigsy

ClioSport Club Member
  T.Turbo
Updates.

Both dci's washed on Thursday. Rinsed using the di vessel, great finish with no watermarks.
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Blue dci passed mot today with no advisories. Mot testers comments - "clean for an old car". Current mileage 204718, not gone up much this month due to using the orange dci.

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I have a few site visits planned at work so mileage will increase quite a bit soon.

Thanks for reading!!
 
Last edited:
Updates.

Both dci's washed on Thursday. Rinsed using the di vessel, great finish with no watermarks.View attachment 1762438View attachment 1762437
View attachment 1762435

Blue dci passed mot today with no advisories. Mot testers comments - "clean for an old car". Current mileage 204718, not gone up much this month due to using the orange dci.

View attachment 1762436
I have a few site visits planned at work so mileage will increase quite a bit soon.

Thanks for reading!!
 

Brigsy

ClioSport Club Member
  T.Turbo
Updates. Blue dci is almost on 207k now as been commuting to Hull quite a bit. No dramas as all motorway driving, Its not a bad drive being honest with the m62 being quiet to Hull.

Almost daily sight this week.
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Give it the blue dci a hoover out a couple of weeks ago. Drivers seat is getting there so need to do something about that soon.
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Also picked up a cheapo trafic/vivaro 1.9dci egr delete to try. The egr is more or less identical on the trafic so might go, ill have a look at it one day soon.
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Mrs has been using the orange dci a bit. It chucked eml on briefly last time she used it which as expected was throttle position sensor track 1 Df071.
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Apparantly it was reading 879% on track 2 :LOL: ill have a look at wiring etc soon.

Thanks for reading!!
 

Brigsy

ClioSport Club Member
  T.Turbo
Updates.

Give the blue dci egr a once over on Sunday as looks a bit more black smokey than usual. Ten min job to remove and examine, looked pretty clean so straight back in. Offered up the egr blank whilst apart, it seemed to be a loose fit and i could imagine it leaking so sacked that off..original egr working is good enough.

Whilst there i changed the airbox for one that @Martin_172 kindly donated. My airbox was well worn round the induction pipe and was causing noise/resonation on overrun and reversing when engine was loaded. The new airbox was in much better condition so fitted that and the new induction pipe that was also in good nick. This cured all airbox rattles and the engine sounds loads quieter.

Airbix fitted, its no show winner under the engine cover😄
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Have also ordered cambelt kit, water pump and aux kit. Cambelt has done 64k so its about due. Xmas job, when i get a spare half day.

Orange clio is in the mrs bad books. She used it the other day and the pedal/limp fault was present for most of the journey..best get it fixed soon or there will be hell on😄

Ive ordered a replacement pedal, will try that first. If no joy, i have an old 182 interior loom to chop the wiring out of to replace bits, and ill check out the white plug of doom for corrosion.

Thanks for reading!!
 

Brigsy

ClioSport Club Member
  T.Turbo
Updates

Mrs was out in the blue clio yesterday and i needed to go out. Id normally jump in the r26 but its got no gearknob on it as its at the trimmers. Rest are sorn apart from the orange dci which is in limp. Best fix it eh!?

Usual fault stored when scanned with clip.
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I bought a new accelerator pedal to fit so had the parts in stock, so should be an easy fix. Could i f**k get the pedal/bar off to swap over, my small puller has went awol so give up before it all broke.

With the defective pedal on the bench, i stripped the cover off to see if repairable. Its 5x posi screws and the cover comes off. The tracks on each potentiometer appeared to be worn but not beyond serviceable. I levered the contacts slightly to add more tension, and cleaned everything up and refitted the cover.

Cycled the pedal through a few presses with ign on and all good. Done 30mile or so yesterday and no limp, appears to be fixed. Simple repair, will see if it lasts.

Thanks for reading!!
 

Brigsy

ClioSport Club Member
  T.Turbo
Updates

The blue dci seemed a bit slower and black smokey recently, bit intermittent as sometimes fine. Not sure if it was actually slower or felt slow after a week of driving the r26 fast as fcuk everywhere at Spa/Germany, but yeah thought it was worth a quick look at.

Stuck torque on it and noted it was making boost ok but bit lazy getting there. Basically when i changed the turbo a while back, i noted boost pressure was a little lower but never done anything about it as its no rocketship.

Anyway had a dry morning so got the smoke kit out to leak test, just incase any boost leaks had developed.
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The boost circuit on dci65 is super simple with no intercooler. Smoked it up and no leaks at all, air tight with the crankcase smoking up as the rings naturally let a bit by even with good compression.

Smokin.
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With the boost circuit declared leak free, i took the egr out and inspected, pretty clean. Took the stainless steel pipe from egr to inlet off to check for soot restrictions and also pretty clean.

Cleaned both and got the mityvac out to check wastegate crack pressure, which was just under 15lbs, cranked the actuator up a bit so just over 15lbs. Also fitted a new airfilter that i got off @plees as the old one was not great/12k old.

Took for test run and boost up a little bit. Feels normal ish, was hard to tell if any better as been driving the megane all day. I will monitor and see how it goes, get the feeling egr might be playing up intermittently or maybe fuel system is a little bit tired. Might be worth logging fuel pressure at some point to see if anything is obvious?

Anyway overall runs good enough. Thats all that counts really.

Thanks for reading!!
 

Brigsy

ClioSport Club Member
  T.Turbo
Updates.

Blue dci passenger rear drum brake started making a right squealing the other day. Brake pedal was still ok ish but not as sharp as it had been and handbrake was a bit w**k.

This is usually due to one of the below issues as i have been there before on several different cars over the last 25 years.

Shoes worn out - were thin ish last time i adjusted.

Shoes need adjusting and drum cleaning.

Rear brake cylinder starting to leak, causing dust to clog up, contaminating the shoes and make loads of noise.

With the brake shoes looking thin last time i adjusted them, i had a set in stock which i stuck in a recent autodoc order, with 2x new cylinders and fitting kit. Also ordered 2x new rear drums. Full monty.

Weather not bad this afternoon, stripped down fast. Gear all over
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Passenger side drum examined, shoes indeed low but not on metal. Noise was due to a leaking brake cylinder and adjustment required, noted shoes looked a bit contaminated. On initial inspection brake cylinder looked ok, but pop the dust seal off and it was full of brake fluid. Pulled it off easy, brake pipe undone and new cyl and shoes on.

All new.
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Went to fit the new drum and it was tight on the backing plate, rubbing as crap aftermarket. This could have been resolved by removing rust off the backing plate and a small chamfer, but then compared abs rings and 10mm smaller in diameter, so no good.

With this fail i measured the original drum. The drum was just under the max tolerance 203mm recorded vs 204mm max so were ok to reuse once again. They needed a clean up, delipped the drum, give the outer a clean up with grinder on knotted wheel and painted in vht black. This was to try and stop the shoes sticking in wet weather, as i believe the drums let a bit of water in due to porosity in the casting. Hopefully a bit of paint might seal.

Shoes adjusted, drum refitted and onto drivers side. Drivers side was OK and still in adjustment but as per brakes always do in pairs. Stuck a new cylinder in as they usually fail shortly after fitting new shoes to take the piss.

Before
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After.
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Drum got the same treatment as above. Easy yet s**t job, i hate the springs on the shoes.

With that part done, i pressure bled the brakes all round, i dont think its been done for 50k or so, so looked pretty grim.
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Brake pedal nice and solid/sharp, and handbrake back to 4x clicks again. Normal service resumed.

Thanks for reading!!
 

Brigsy

ClioSport Club Member
  T.Turbo
Updates.

Fired the orange clio up to move it, to get the breaker megane 225 out. Starts up as usual and idling for a couple of mins in usual chuggy fashion from cold, its never ran great from cold but has been like that for 45 thousand miles.

I hear idle pick up suddenly and smooth out, and without even looking i know the fcuker has put the eml light on/went into limp. Look at dash and eml/glow plug light is shining brightly.

Plug in clip and laptop goes flat so stick Renolink on for a look.

No idea if the codes mirror clip but same ddt2000 database. Says injector 3 combustion.
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Look in the accelerometer page and injector 3 certainly reading something different to the rest. Taking a wild guess its an injector thats not too happy or injector seal.

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Cleared dtc's and runs as normal again. In hindsight i should have left it and read it with clip.

Might be time for a new injector or seal. Ill give it a bit of use next week and see if it repeats it.
 


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